A lot has happened since I've been able
to post anything on the blog, so time for an update, all the way back
to Wednesday June 12. “Some Lucky” left to go down the east side
of Gwaii Haanas. Our intermittent electrical problems continued to
plague us, so after we'd returned the car at noon, we spent most of
the afternoon working on trying to trace the problem....again....and
again....and again. I found a local marine electrician who was very
busy on the fishing fleet in preparation for the upcoming salmon
opening on the 20th, but he agreed to come over and have a
look at the end of his day. Geoff (the electrician) finally showed
up a little after 6 PM and started tracing all of my
connections.....he found a suspect wire running from the negative bus
to the negative switch panel – he advised it was much too small for
its needs, and that it be replaced by a larger one. I agreed, and he
supplied me with some #6 wire to replace the smaller #16 in place,
and he connected the lug connections onto it, and left me to connect
and run the wire through. I also decided to do the same thing with
the positive side of things. I managed to get most of this done,
with the understanding that Geoff would return in the morning to
check out the connections and voltages. By this time it was 1930, so
I quit work and walked up to the head of the dock to join Ray in
Howlers Bar (the only pub in town) to watch the end of the first game
of the Stanley Cup Finals. I'm not a big hockey fan, but I enjoyed
the action in this game, which went into two overtime periods before
the Chicago win. The following morning, Geoff arrived at 0830 to
check my work and the connections, and declared our system fit to
use. By 0930 we were motoring out of the harbour in sunny and warm,
and calm conditions. But a little over a mile out of the harbour,
our engine overheat warning went off. We shut down the engine and
checked the water intake – clear. Then we checked the water pump
and the impeller inside it, and the belt which drives it – all OK.
So we sailed back slowly, and at the harbour mouth, were able to
motor back into the dock (the engine had cooled enough for a short
run). A snake through all of the various water lines, a recheck on
the intake, water pump, impeller all proved no problems....so I
disconnected and cleaned the heat exchanger, with still no positive
results. The last part of the cooling system is a large elbow used
to mix the exhaust gases with the coolant water, but requires a very
large wrench to remove and clean it. The pipe wrench we have is big
enough...but too thick. The other boaters around us were helpful in
lending various tools and wrenches, but nothing fit. I walked all
over town, renting a large adjustable wrench which ended up not
fitting. A local fisherman, Lindsay, was very helpful in suggestions
and then in driving me around to various shops in town, finally
finding the right wrench (which we borrowed from a machine shop in
town in return for a case of beer). The wrench fit, and started to
loosen the fittings, but by then it was getting late – so we called
it a day, had supper, and an early night.
Saturday morning dawned bright and
sunny yet again – perhaps my impressions of a cold and rainy Haida
Gwaii were mistaken! I was able to finally remove the fitting with
the wrench, and get it all cleaned. But when all was back together
again, to my complete frustration, we still had no coolant water
making through the system! Back to the beginning – this time, I
removed the hose from the intake water pipe, instead of checking the
opening at the top....and found some seaweed clogging the hose. This
fitting had been replaced last fall by Stone's Boatyard, and I had at
the time complained that it was a 90 degree elbow fitting....but they
insisted it was necessary for the hose to fit properly. I should
have stood my ground, as a straight fitting would have been
immediately evident for a clog, and would not have created the
seaweed trap in the first place! At any rate, this fixed the
problem....and I was now quite confident that the entire cooling
system was in good order. It was too late to leave today, so we
spent another evening at Howler's Pub watching game two, which also
went into overtime.
So enough with the fixing – it is
certainly time to get exploring again, or at least run out a scouting
trip to check out the area before Ray's wife Kathy flies in to join
us for five days, on the 20th. No pictures to go with this entry....but I promise a bunch of them in the next entry to update everybody to the present time!
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